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Gulf of mexico fire
Gulf of mexico fire












gulf of mexico fire

The flow of gas into the engine rooms through the ventilation system created a potential for ignition which the rig’s fire and gas system did not prevent.

gulf of mexico fire

  • After the well-flow reached the rig it was routed to a mud-gas separator, causing gas to be vented directly on to the rig rather than being diverted overboard.
  • Over a 40-minute period, the Transocean rig crew failed to recognise and act on the influx of hydrocarbons into the well until the hydrocarbons were in the riser and rapidly flowing to the surface.
  • The results of the negative pressure test were incorrectly accepted by BP and Transocean, although well integrity had not been established.
  • The cement and shoe track barriers – and in particular the cement slurry that was used – at the bottom of the Macondo well failed to contain hydrocarbons within the reservoir, as they were designed to do, and allowed gas and liquids to flow up the production casing.
  • The report – based on a four-month investigation led by Mark Bly, BP’s Head of Safety and Operations and conducted independently by a team of over 50 technical and other specialists drawn from inside BP and externally – found that:

    Gulf of mexico fire series#

    Rather, a sequence of failures involving a number of different parties led to the explosion and fire which killed 11 people and caused widespread pollution in the Gulf of Mexico earlier this year.Ī report released by BP today concludes that decisions made by “multiple companies and work teams” contributed to the accident which it says arose from “a complex and interlinked series of mechanical failures, human judgements, engineering design, operational implementation and team interfaces.” No single factor caused the Macondo well tragedy.














    Gulf of mexico fire